Weird, when I looked up M4514 it came back as a late 69s big block pump. I thought 30gph was good for more than what I'm making? But if MKIV spec'd a 40gph I can pursue that.
As for the suction side, rher'd only be a small section in question as a majority of the mid section hard line has been replaced. Wouldn't a guy have a leak if that were to blame? I can say for sure it's not the cause of the car not running, but may still rear its head with a good pump if that's to blame. The tank and sock are pristine, they were out back in December and thinking back, this problem predates that by quite a bit. I seem to recall my dad lamenting the thing running out of fuel back around 2018, I believe he got there because he had the vacuum modulator cranked to the moon and back. I had to fiddle with the governor to get it to wind up hard enough for that.
As for the suction side, rher'd only be a small section in question as a majority of the mid section hard line has been replaced. Wouldn't a guy have a leak if that were to blame? I can say for sure it's not the cause of the car not running, but may still rear its head with a good pump if that's to blame. The tank and sock are pristine, they were out back in December and thinking back, this problem predates that by quite a bit. I seem to recall my dad lamenting the thing running out of fuel back around 2018, I believe he got there because he had the vacuum modulator cranked to the moon and back. I had to fiddle with the governor to get it to wind up hard enough for that.
Last edited: