Operation Lipstick on a Pig

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So, I think the belt route I had was pulling away from the tensioner. I rerouted it, and came up with a shorter belt by 3". Only problem with that is the alternator wrap is greatly reduced. Stay tuned.....
I also came up with some other issues with the keyless: it's not recognizing the tach output from the PCM, doorlocks don't work (I wired it without testing), etc...

TURNA, there's no rod knock; it's got 90psi of pressure with 5w-30 and the ZZP pressure kit.😀
 
Awesome!
 
Got the dash back in, and did not turn out anywhere close to what I imagined. This is definitely temporary! But, it's in nonetheless.
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