Our replacement radiator showed up Friday afternoon...
It looks to be well built and we really like the lifetime warranty. We wish it had been made in the USA and wish that the USA made radiator that we had, had held up better but oh well.
Towards the end of the day I called Eckler's to check on the status of my door panel barrel nut order. It didn't get picked up until 3:30 Friday and we wouldn't have it until Monday. I was not happy. I paid next day air shipping and paid extra for them to expedite processing the order. I decided I could live (would have to live) with getting them around 10 AM on Monday (when the FedEx truck normally comes by). More on that later.
Saturday morning we started with installing the radiator. It was pretty straight forward but the new radiator wasn't as tall as the old one so we had to cut down our lower fan mounting brackets and drill new holes in them where they mount to the lower portion of the core support. I elected to repaint those brackets rather than put them back on the car with the ends of them bare so we had to wait for the paint to dry.
While we did, we worked on the air intake. One of the places where we were pretty sure we were getting some unmetered air was where the crankcase breather hose tied into the air intake elbow. We had initially tried to use a rubber grommet and a vacuum fitting to make the connection but weren't able to make the grommet and fitting fit in the hole in the elbow tight enough. We ended up resolving this by using a pipe thread hose barb fitting and a few washers for spacers. The barb fitting threads right into the elbow. The spacers are only needed since there is an unthreaded shoulder on our fitting below its hex. We used a little clear silicone between each washer, between the intake elbow and the lower washer and between the fitting and the upper washer. It turned out well...
I also worked on the lock switch for the driver's side door to get ready to put it in the panel. Our aftermarket switches were not of the utmost quality. The pins wanted to push out when you put the wiring connector on the switch. Also, the switch had the tendency to just come apart when you pressed lock or unlock. I removed the two pressed in pins and glued them in with super glue. I also glued the back of the switch to the bezel. It sounds easier than it was. We also worked on improving how the passenger roof rail weatherstrip was glued down at its front end where it meets the front of the door shell.
We also did quite a bit of running around on Saturday, both running for parts and for stuff for my nephew's 22nd birthday. We had family over that evening to BBQ and celebrate.
Sunday we went back to installing the radiator and fans. We got the fans back in the car with our modified lower mounting brackets and discovered the radiator was fitting loosely in the rubber saddles (would wiggle fore and aft). It turns out the tanks for the old radiator were wider than the new one and we had modified our saddles (urethane) to accommodate it. Fortunately I had a set of new urethane saddles for the GP over at the storage. I went and grabbed them and we were able wrap up the installation of the radiator.
We got the air intake reinstalled and cranked the car up. It didn't race on cold start up which was a good sign we had been successful with our quest to remedy the un-metered air. We took the car for a test drive. It was still morning. It was a fun drive. We had a lot of wins. The un-metered air issue was solved. The rear brake adjustment was a stunning success. The car's brakes were dramatically improved and the emergency brake was completely effective. The steering wheel was straight. The windows were going up and down smoothly. I enjoyed having a door panel, and arm rest on my side. It was awesome. We got the car back home and did a little more work to make the car better. Sean got under the car and touched up the paint on the tie rod end adjusters. I worked on oiling the hood hinges and hood latch. I know this sounds like a small thing but it was transformative. The hood had gotten pretty stiff. I used an oil can with 30 weight non-detergent motor oil to lube the hood hinges. I held a paper towel under each pivot point and flooded each with oil. It took some time but worked way better than using aerosol white lithium grease. At this point our list of things we wanted to do to the car was getting short. The biggest thing left was to install the driver's side door panel. We were just waiting for the panel clip barrels to show up.
Monday was a short day. We had plans to go to the Astros home opener that afternoon. We waited all day for those barrels to show up. They never did. In the meantime we programmed a new, smaller remote for the garage door to the Camaro bay. We did some clean up in the Camaro bay. Sean put Rain-X on all of the exterior glass. We worked on coming up with some speaker grills for the front speakers. If you remember, Sean and I managed to shoehorn 6"x9" speakers in the stock kick panels. They are so tight to the toeboards, HVAC case and the E-brake mechanism that the grills that came with them would not fit (way too big). We ended up cutting the mesh out of the grills that came with the speakers and then painting them with low gloss black. We also diagnosed why the cruise control wasn't working. It turned out that we weren't getting +12V to the cruise module that runs through the brake light switch and the clutch pedal momentary switch. My back has been tender all week so I didn't want to get under the dash ahead of the ballgame. That was our Monday. We left for the ballgame at 3:00. The barrel nuts were delivered at 3:40. I was pissed about that.
Sean and I had a goooood time at the ballgame last night. We got a little slower start this morning. Sean beat me out there and got the painted speaker grills installed. It's hard to get a picture on these but here you go....
We just fastened them with 3M two-sided tape. You really can't see them. We just want to protect the speakers from feet, mainly those of the passengers.
Next we worked on the driver's side door panel. It was a bit of a fight. We ended up having to plastic the car up again and trim our opening for the door lock switch on the upper end. The OE connector was hitting the door shell. The armrest fought. I even poked an un-needed hole in the door panel at the front end of the armrest/door pull but thankfully it is covered by the armrest. With some perseverance we got the driver's side door panel buttoned up....
We took a short break from the car and swapped out the blower motor in my brother's 02 GMC Sierra. I had been wanting to get to that all week. Then we got back on the car. Now that we had door panels on both sides, we optimized the tune on the stereo. We were able to do all of it with the head unit (fader, bass, treble, mid, subwoofer level, etc.). We've got it sounding really good. Then we both got under the dash and together (not at the same time, obviously) we got the brake light and clutch pedal switches adjusted and got the cruise working again. This was everything on our list. It was getting close to the rush hour so we only took the car for a short victory lap but it was fun.
The car is as complete as it has ever been, going all the way back to 1985. It is running very well and everything works. It's painted and the interior is complete. As I said previously, Sean and I believe these cars are never 100% finished but this car is extremely close. It was a hell of a week. We're both thrilled. Sean is going to drive the car to work tomorrow. I know he is going to enjoy it.
That's it for now gents. Thanks for following along. I don't know when the next update will be, but there will be one. Until then.....
Best,
Jared